The 1899 Locomobile Steam Car Replica, known as the Lykamobile is a full scale live steam automobile manufactured in 24 kits. This kit is available from a company called "Steam Traction World" located in Daventry, United Kingdom. Each kit is to be manufactured and sent once a month for 24 months. However for cost considerations I have chosen to have my kits batched and dispatched in larger crates to the United States (Topsail Beach, NC).

Specifications:
• Length 7ft 2.6in • Height 5ft 3in • Width 4ft 7.1in • Weight 904 lbs.• Water Tank Capacity 12 Gallons • Fuel Tank Capacity 7.3 Gallons

Construction:

CHASSIS Tubular steel fabrication, combination weld, bolted and silver solder.
STEERING “Ackerman” design tiller steering.
DIFFERENTIAL & DRIVE Spur gear differential similar to the original Locomobile, drive shaft and bearings.
WHEELS & TYRES Single tube pneumatic, treaded.
BREAKING SYSTEM Disc brake system.
ENGINE 21/4" diameter, 3" stroke modified “Hackworth” valve gear.
WATER FEED Twin mechanical pump.
BURNER Fuelled by diesel.
BOILER Multi Fire Tube, fully constructed and complete with necessary paperwork and inspected by notified body.
BODYWORK & SEATS Wooden with steel frame, seating capacity of 2 persons, with turned decorative spindles with leather style upholstery.
Gears: forward and reverse.
Assemble with hand-tools only
Step-by-step instructions
Technical service and help-line backup
Designed on ‘Solidworks’ CAD
Manufactured on modern CNC machines for build accuracy and high quality


Tuesday, November 10, 2020

Lyka Kit #22 Final Kit - Part 2

Steam Traction World is supposed to be sending us Steaming Instructions that have not been written up yet, so being a little impatient I decided to hookup my air compressor to the inlet feed pipe which is located on the top of the boiler. This is a 3/8" pipe thread that will eventually be plugged once the first initial fill of water is done. I set the air pressure to 100 psi. Below is a video of the engine running in reverse. The engine uses a modified Hackworth Valve Gear and per the design the engine actually runs smoother in reverse. I suspect the engine has more power in forward though. I used some Chevron Meropa 680 gear oil for the steam oil. Still waiting to hear from Steam Traction World for a specification on the proper oil to use.

Very exciting to see the engine run at last !!

Now that I have the system pressurized I can start to chase down any leaks. Plain old dish washing soap and water is applied to all the fittings. I notice a few leaks here and there. One leak is at the interface between the two components for the throttle regulator valve.
I tried to use the Steam Seal Joint compound and this did not work. The threads are straight threads. I had to resort to High Temperature Silicone Gasket Maker - this did work.


I had a leak at the pressure gauge and this was solved with one rotation of the pressure gauge. Also I can hear inside the boiler at the inlet feed pipe a small leak. I had problems with this pipe fitting/thread and I suspect that the pipe thread was over cut and the taper was a bit too small. I will monitor this once the boiler is up to temperature to see if the expansion of the boiler seals the leak. It is a small leak and possibly won't be an issue with steam. I have also notice small leaks around the interface of the valve chest bolted to the cylinder blocks and again I will monitor this. It would be a big job disassembling to apply another amount of steam sealant there. All of the leaks so far have been very minor.

Next I decided that I was not too thrilled with the way Steam Traction World mounted the cylinder blow-off valve. This valve is mounted to the backside of the main floor board with 4 lag bolts. Any time that you want or need to take the floor board out would necessitate disassembly of the 4 lag bolts from underneath the chassis. My solution was to make a bracket and mount the valve to the frame. Below are the images for this.



The cross bar bracket is bolted to the frame and is flush with the frame. I used flat head countersink screws. And finally for this update, the last item was to secure the 1/4 inch copper tubing that goes to the pressure gauge to the frame. A simple strap was made and I used a frame cross-member bolt to secure it. I felt that this was necessary to prevent a rattle. No doubt I probably wouldn't be able to hear it, but I eliminated it anyway.
And one last detail: I hooked up the chain and decided that I needed to get an offset link (half link). The chain is just a tad too long (by a half link), so I will have to take a full link off the chain and then use the half link to reduce the slack. Without this, the chain would be slapping around beating "things" up.
Trials and Tribulations Part 2 will be final details for the floor boards. 

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